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      British 
                                        Overseas Airways flight 712 was 
                                        scheduled to leave London's Heathrow 
                                        airport bound for Sydney at 3:15pm on 
                                        April 8, 1968. On the flight deck was 
                                        Captain C W R Taylor, First Officer F B 
                                        Kirkland, Second Officer J C 
                                        Hutchinson,and Engineer T C Hicks as 
                                        well as Check Captain G C Moss. Along 
                                        with a cabin crew of six, there were 116 
                                        passengers on board the Boeing 707 that 
                                        afternoon. 712 departed Heathrow at 
                                        3:27pm and just after the landing gear 
                                        was retracted, there was a shudder 
                                        throughout the airframe and a loud bang 
                                        from the port side. 
                                        
      
                                         
                                          
                                            
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                                             712's Engine Falls Away
 |  The 
                                        port inboard engine throttle lever moved 
                                        back towards idle and the instruments 
                                        indicated that the engine had failed. 
                                        Taylor called for the engine failure 
                                        checklist and Hicks began the drill. As 
                                        he pulled the throttle to full idle, the 
                                        landing gear warning horn sounded (it 
                                        sounds when the landing gear is up and 
                                        the throttle is retarded). Hicks and 
                                        Moss both reached to switch off the 
                                        warning bell, but Moss hit it first and 
                                        Hicks, not realizing that Moss had done 
                                        so, inadvertently shut off the engine 
                                        fire alarm warning as well. No fire 
                                        drill was started. A few moments later, 
                                        Moss looked out the port side window and 
                                        saw that the engine was indeed on fire 
                                        and told Taylor that he should head back 
                                        to the airport as soon as possible. 
                                        Taylor then noticed that the engine fire 
                                        warning light was illuminated and 
                                        commanded the fire drill be initiated. 
                                        Hicks began the engine fire drill as 
                                        Kirkland called Heathrow to declare the 
                                        emergency and Taylor began his turn back 
                                        to the airport. The fire was so strong 
                                        that, before Hicks could complete the 
                                        engine fire drill, the fire burned 
                                        through the mounting structure and fell 
                                        away as it was designed to do. The fire 
                                        still burned and the loss of the engine 
                                        caused a loss of hydraulic power to the 
                                        landing gear and flaps. Luckily, Taylor 
                                        had extended the landing gear and the 
                                        flaps stopped 3 degrees short of the 
                                        fully extended position. Taylor managed 
                                        to get the 707 back on the ground 
                                        smoothly and used reverse thrust on the 
                                        two outboard engines to slow the 
                                        aircraft. Unfortunately, the reverse 
                                        thrust also deflected the flames toward 
                                        the fuselage. As soon as the aircraft 
                                        stopped, Taylor ordered engine fire and 
                                        shutdown drills on the remaining three 
                                        engines, but an explosion on the port 
                                        wing caused him to order the cockpit 
                                        abandoned. Meanwhile, cabin crews had 
                                        prepared for the emergency exit, but the 
                                        explosion and resulting fire prevented 
                                        them from using the port side and rear 
                                        exit doors. Both Hicks and Taylor had 
                                        exited the aircraft and were helping 
                                        passengers on the ground. The rest of 
                                        the flight crew, after being blocked 
                                        from exiting out the front galley doors, 
                                        left via the cockpit. Evacuation 
                                        remained somewhat orderly and all but 
                                        five people were able to exit the 
                                        aircraft before it was overcome by fire 
                                        and smoke and totally lost. 
       
                                            Clearly 
                                        some sort of malfunction had sparked a 
                                        massive fire within the port inboard 
                                        engine. Puzzling to the investigators 
                                        was the magnitude of the fire and the 
                                        crew's inability to control or 
                                        extinguish it. In retracing 712's flight 
                                        path, investigators found fragments of 
                                        the engine's compressor blades near the 
                                        departure end of the runway. Further 
                                        along, a piece of the engine cowling 
                                        which had been blown off and portions of 
                                        the number 5 compressor wheel rim. 
                                        Examination of the engine after recovery 
                                        showed that the number 5 compressor 
                                        wheel had disintegrated due to fatigue, 
                                        it's debris being blown through the 
                                        engine and severing the fuel feed lines 
                                        and allowing fuel to flow freely into 
                                        the engine. Examination of the aircraft 
                                        after the fire was extinguished showed 
                                        that none of the fire shutoff handles 
                                        had been pulled nor had the fuel boost 
                                        pumps been turned off. Pulling the fire 
                                        shutoff handles closes the fuel shutoff 
                                        valve for that engine, shuts off the 
                                        supply of hydraulic oil, and arms the 
                                        fire extinguishers. The investigation 
                                        then turned to why the crew had failed 
                                        to complete the drill as required. The 
                                        first clue came in Hick's accidental 
                                        disarming of the engine fire alarm bell. 
                                        Since the bell did not sound, it seems 
                                        that the crew did not initially believe 
                                        the emergency was a fire. When Moss 
                                        pointed out the fire, it is thought that 
                                        the crew had a miscommunication during 
                                        the command to start the engine fire 
                                        drill. Hicks had already started the 
                                        engine shutdown drill and then simply 
                                        continued with the drill as it was the 
                                        same as the engine fire drill with the 
                                        exception of pulling the handle, the 
                                        first item. Since the checklist had 
                                        already been started, it is thought that 
                                        Taylor believed his crew had already 
                                        pulled the handle. Though the fire light 
                                        remained on, when the engine feel away 
                                        from the aircraft, the light would have 
                                        gone off and the crew's attention would 
                                        be lost. Because of this, BOAC combined 
                                        it's engine failure and fire drills into 
                                        one checklist, all of which had to be 
                                        confirmed instead of beginning with 
                                        memory items. 712 Burns on the Ground
 
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