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British
Overseas Airways flight 712 was
scheduled to leave London's Heathrow
airport bound for Sydney at 3:15pm on
April 8, 1968. On the flight deck was
Captain C W R Taylor, First Officer F B
Kirkland, Second Officer J C
Hutchinson,and Engineer T C Hicks as
well as Check Captain G C Moss. Along
with a cabin crew of six, there were 116
passengers on board the Boeing 707 that
afternoon. 712 departed Heathrow at
3:27pm and just after the landing gear
was retracted, there was a shudder
throughout the airframe and a loud bang
from the port side.
712's Engine Falls Away |
The
port inboard engine throttle lever moved
back towards idle and the instruments
indicated that the engine had failed.
Taylor called for the engine failure
checklist and Hicks began the drill. As
he pulled the throttle to full idle, the
landing gear warning horn sounded (it
sounds when the landing gear is up and
the throttle is retarded). Hicks and
Moss both reached to switch off the
warning bell, but Moss hit it first and
Hicks, not realizing that Moss had done
so, inadvertently shut off the engine
fire alarm warning as well. No fire
drill was started. A few moments later,
Moss looked out the port side window and
saw that the engine was indeed on fire
and told Taylor that he should head back
to the airport as soon as possible.
Taylor then noticed that the engine fire
warning light was illuminated and
commanded the fire drill be initiated.
Hicks began the engine fire drill as
Kirkland called Heathrow to declare the
emergency and Taylor began his turn back
to the airport. The fire was so strong
that, before Hicks could complete the
engine fire drill, the fire burned
through the mounting structure and fell
away as it was designed to do. The fire
still burned and the loss of the engine
caused a loss of hydraulic power to the
landing gear and flaps. Luckily, Taylor
had extended the landing gear and the
flaps stopped 3 degrees short of the
fully extended position. Taylor managed
to get the 707 back on the ground
smoothly and used reverse thrust on the
two outboard engines to slow the
aircraft. Unfortunately, the reverse
thrust also deflected the flames toward
the fuselage. As soon as the aircraft
stopped, Taylor ordered engine fire and
shutdown drills on the remaining three
engines, but an explosion on the port
wing caused him to order the cockpit
abandoned. Meanwhile, cabin crews had
prepared for the emergency exit, but the
explosion and resulting fire prevented
them from using the port side and rear
exit doors. Both Hicks and Taylor had
exited the aircraft and were helping
passengers on the ground. The rest of
the flight crew, after being blocked
from exiting out the front galley doors,
left via the cockpit. Evacuation
remained somewhat orderly and all but
five people were able to exit the
aircraft before it was overcome by fire
and smoke and totally lost.
712 Burns on the Ground
Clearly
some sort of malfunction had sparked a
massive fire within the port inboard
engine. Puzzling to the investigators
was the magnitude of the fire and the
crew's inability to control or
extinguish it. In retracing 712's flight
path, investigators found fragments of
the engine's compressor blades near the
departure end of the runway. Further
along, a piece of the engine cowling
which had been blown off and portions of
the number 5 compressor wheel rim.
Examination of the engine after recovery
showed that the number 5 compressor
wheel had disintegrated due to fatigue,
it's debris being blown through the
engine and severing the fuel feed lines
and allowing fuel to flow freely into
the engine. Examination of the aircraft
after the fire was extinguished showed
that none of the fire shutoff handles
had been pulled nor had the fuel boost
pumps been turned off. Pulling the fire
shutoff handles closes the fuel shutoff
valve for that engine, shuts off the
supply of hydraulic oil, and arms the
fire extinguishers. The investigation
then turned to why the crew had failed
to complete the drill as required. The
first clue came in Hick's accidental
disarming of the engine fire alarm bell.
Since the bell did not sound, it seems
that the crew did not initially believe
the emergency was a fire. When Moss
pointed out the fire, it is thought that
the crew had a miscommunication during
the command to start the engine fire
drill. Hicks had already started the
engine shutdown drill and then simply
continued with the drill as it was the
same as the engine fire drill with the
exception of pulling the handle, the
first item. Since the checklist had
already been started, it is thought that
Taylor believed his crew had already
pulled the handle. Though the fire light
remained on, when the engine feel away
from the aircraft, the light would have
gone off and the crew's attention would
be lost. Because of this, BOAC combined
it's engine failure and fire drills into
one checklist, all of which had to be
confirmed instead of beginning with
memory items.
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