Northwest flight 255 was preparing for takeoff on the evening of August 
      16, 1987. Bound for Phoenix and continuing on to Orange County, the DC-9 
      was carrying 148 passengers and six crew members. The aircraft was cleared 
      for takeoff on Detroit Metro's runway 03C and began its takeoff roll. 
      After an longer than normal roll, the aircraft lifted off and immediately 
      began rocking laterally. It only gained 50ft in altitude before clipping a 
      light pole with its left wing. It hit a number of other light poles and 
      then clipped the roof of a building, rolling past 90 degrees and then 
      slamming into the ground and bursting in flames. Everyone aboard the 
      aircraft was killed with the exception of a four year old girl. Two 
      motorists who were driving along a highway where wreckage was strewn were 
      killed also.
      
                                        ......Examination of the wreckage showed 
                                        no signs of any system malfunctions. The 
                                        only significant find in the wreckage 
                                        was that both the slats and flaps were 
                                        retracted. Both would normally be 
                                        extended during takeoff. Examination of 
                                        the cockpit also showed that the flap 
                                        handle was in the retracted position. 
                                        This was further confirmed by recovery 
                                        of the FDR. Readout of the CVR showed 
                                        that the crew had neither called for nor 
                                        completed the taxi checklist, on which 
                                        the extension of the slats and flaps are 
                                        the first item. Just as the aircraft was 
                                        pushed back from the gate, the first 
                                        officer, who would have normally started 
                                        the taxi check at that time, was instead 
                                        copying the lastest ATIS, which had just 
                                        been updated. 
                                        By the time he was 
                                        done copying, the aircraft was already 
                                        taxiing to the runway and it's possible 
                                        that he believed the extension had 
                                        already been done. The captain is 
                                        responsible for calling for the 
                                        checklists, though the captain of 255 
                                        did not call for the after-start, taxi, 
                                        or pre-takeoff checklists. The crew also 
                                        had difficulty taxiing to the proper 
                                        runway even though they had flown out of 
                                        Detroit several times before. The DC-9 
                                        is equipped with CAWS which should have 
                                        alerted the crew to the improper 
                                        configuration, but no such warning was 
                                        heard on the CVR. This was accounted to 
                                        a power loss prior to taxi, though it 
                                        could not be determined whether it was 
                                        intentional or accidental. 
                                        This improper 
                                        configuration severely degraded the 
                                        aircraft's climbing performance. The 
                                        stick-shaker activated less than one 
                                        second after lift-off and continued 
                                        throughout the short flight. At the time 
                                        of the incident, the weather was good 
                                        though there were storms in the 
                                        immediate vicinity of the airport and 
                                        windshear advisories were issued. It's 
                                        possible that the crew believed 
                                        themselves to be caught in windshear 
                                        which was evidenced by the captain's 
                                        increased pitch-up, which is standard 
                                        windshear avoidance procedure. 
                                        Had the crew lowered 
                                        the nose and extended the flaps and 
                                        slats, the accident probably could have 
                                        been avoided. It was speculated that the 
                                        crew may have been hurried in an effort 
                                        to depart before the weather got any 
                                        worse. Also, they may have been rushed 
                                        in an effort not to miss the noise 
                                        curfew at Orange County, their final 
                                        destination.