Southern 
                                        Airways flight 242 was operating from 
                                        Huntsville to Atlanta on the afternoon 
                                        of April 4, 1977. On the flight deck of 
                                        the DC-9 that day was Captain Bill 
                                        McKenzie and First Officer Lyman Keele. 
                                        Two flight attendants and 81 passengers 
                                        were also aboard for the short flight. 
                                        The weather that afternoon was far from 
                                        pleasant, the area forecast predicting 
                                        scattered thunderstorms, some severe 
                                        with icing, turbulence, and hail. There 
                                        were two Tornado Watches in effect as 
                                        well as a SIGMET predicting severe 
                                        thunderstorms reaching up to 58,000ft 
                                        extreme turbulence, wind gusts in excess 
                                        of 70kts, and large hail. 
                                        
      
      
      The crew had 
                                        flown the same route outbound earlier 
                                        and had experienced heavy rain and hail, 
                                        not pleasant, but by all means 
                                        manageable. The forecast for their 
                                        arrival in Atlanta called for overcast 
                                        layers down to 2700ft and winds gusting 
                                        to 40kts. At 3:54pm, with rain falling, 
                                        242 departed Huntsville. Four minutes 
                                        later, they were handed off to Atlanta 
                                        Centre. Atlanta Centre was at the time 
                                        talking to TWA and Eastern flight crews 
                                        who were passing through the SIGMET 
                                        area. 
                                        
                                        
                                        
                                        
                                        
                                        The 
                                        Eastern crew reported that the ride 
                                        "...wasn't too comfortable, but we 
                                        didn't get into anything we would 
                                        consider the least bit hazardous." A few 
                                        minutes later, 242 was instructed to 
                                        descend and maintain 14,000ft. The crew 
                                        acknowledged, but four further 
                                        transmissions went unanswered, finally 
                                        answering "standby" to a fifth call. 
                                        Atlanta then instructed 242 to maintain 
                                        15,000ft to which the crew replied "OK..we 
                                        just got our windshield busted 
                                        and...we'll try to get it back up to 
                                        15...we're 14." Crash Site of 242.
                                        
                                        This was followed shortly by "Our left 
                                        engine just cut out." Thirty seconds 
                                        later, the crew reported "The other 
                                        engine's going too!" 242 asked for an 
                                        immediate vector to a clear area and 
                                        Atlanta instructed the crew to maintain 
                                        it's present heading and contact Atlanta 
                                        Approach. Atlanta continued to try to 
                                        contact 242, but in the next three 
                                        minutes, all of it's calls went 
                                        unanswered. Then 242 came up on Approach 
                                        frequency reporting that it had lost 
                                        both it's engines and needed a vector 
                                        from it's present position at 7,000ft. 
                                        Approach instructed 242 to turn right to 
                                        a heading of 100 for a straight-in 
                                        approach to runway 11 at Dobbins Air 
                                        Force Base. At this point, 242 was 20 
                                        miles west of Dobbins.  
                                        
                                        
                                        After several 
                                        minutes of continued discussion with 
                                        Atlanta Approach, after descending 
                                        through 4,600ft, 242 asked if there was 
                                        a closer airport than Dobbins. Approach 
                                        responded that Catersville airport was 
                                        currently 10 miles north of 242's 
                                        position and 242 asked to be vectored 
                                        towards it. 242 was instructed to turn 
                                        left to 360 and asked for information on 
                                        the airport. Just after Approach 
                                        finished reporting the information on 
                                        Catersville, 242 replied with "We're 
                                        putting it on the highway...we're down 
                                        now to nothing!" 242 was now descending 
                                        over Georgia's State Highway 92, a 
                                        narrow two lane highway flanked on both 
                                        sides by tall pine trees. The DC-9 
                                        clipped a tree with it's port wing and 
                                        then struck an embankment, breaking up 
                                        and bursting into flames and ploughing 
                                        into a service station before coming to 
                                        a stop. Of the 81 passengers on board, 
                                        60 were killed along with the pilots and 
                                        eight people on the ground.
                                        
                                        ......Recovery of the wreckage showed 
                                        extensive hail impact on the tail 
                                        surfaces and engine nacelles. The fan 
                                        blades of both engines showed denting 
                                        due to hail as well. The low-pressure 
                                        compressors were severely damaged, with 
                                        bent and broken blades. In addition, the 
                                        turbines had overheated. Wreckage of 242
                                        
                                        
                                        One of the survivors reported there was 
                                        severe turbulence and heavy rain 
                                        followed by a lightning strike on the 
                                        port wing and hail. He also reported 
                                        hearing popping and surging before the 
                                        engines failures. Water ingestion tests 
                                        of the engines showed that, at flight 
                                        idle, ingestion rates of over 18% caused 
                                        the engine rpm to decrease sufficiently 
                                        to cause generator cutout. This was 
                                        evident in two power losses recorded on 
                                        the FDR and CVR. In addition, test 
                                        showed that, if the throttle was 
                                        advanced to a high power setting, the 
                                        resulting surge could cause bending and 
                                        breaking of the low-pressure compressor 
                                        blades.  
                                        
                                        
                                        This was evidenced in the engine 
                                        by damage of the blades and subsequent 
                                        ingestion of the fragments into the 
                                        high-pressure compressor, causing engine 
                                        failure. The turbine overheat damage was 
                                        produced by high-power settings after 
                                        compressor damage. It was therefore 
                                        determined that heavy rain ingestion, 
                                        not hail ingestion, was responsible for 
                                        the engine failure. Review of the radar 
                                        images of the accident area and the FDR 
                                        showed that 242 actually flew right 
                                        through the most severe part of the 
                                        thunderstorm. 242 was equipped with 
                                        weather radar, but the CVR picked up 
                                        discussion of a "hole" just prior to the 
                                        cell penetration. It is thought that 
                                        what the crew saw was a "contour hole", 
                                        caused by the intensity of the rainfall 
                                        being so severe that the weather radar 
                                        could not accurately display it.  
                                        
                                        
                                        This 
                                        phenomenon apparently misled the crew 
                                        into thinking they could penetrate the 
                                        storm front through a hole. The National 
                                        Weather Service had detailed information 
                                        about the storm area which was available 
                                        prior to 242's departure from Hunstville, 
                                        but Southern's dispatch office was 
                                        unaware of the the storm data and did 
                                        not pass anything on to 242.